Since I registered Oldbike I have been trying to use it as
much as possible in a sort of commissioning process just to see what issues
come up. Some of the things that have
come up I have already talked about in other posts because they were big issues
that required an entire post or two to cover what I did to rectify the
issue. With this post I just want to
cover some of the other little things that have come up as I have been
“commissioning” Oldbike.
I work rotating 12 hour shifts that start or end on the 7s this early in the year I have been commuting in the dark (yes those rides have been cold) one thing that became immediately evident the first morning that I rode the bike to work was that the backlight for the tachometer was burned out. You would never notice it during the day so that was the first thing that I decided to fix. Unfortunately I didn’t take a picture of the tach in the dark with the light burned out but it was hard to see in the early morning with my tinted shield.
There is only one bulb in the back of the each dial
gauge. Getting them out is as simple as
removing the two nuts on the back of each gauge and pulling out the rubber
socket that holds the light bulb.
The bulbs in the my speedo and tach were the original Toshiba bulbs bearing the numbers A12V3.4W (basically calling out that they were for a 12 volt system and that the bulb rating was 3.4 watts) on it this bulb is not made any more so I took the bulb to Batteries (& Bulbs) Plus nearby and they found the most comparable replacement they could with a matching sized base and a slightly larger bulb but that would be the tiniest bit brighter (3.6 watts Vs. 3.4 watts) than the stock ones were but not tax the electrical system any more. The replacements were EiKO brand Model #1893.
They did exactly what they were supposed to do, it will be nice to be able to tell what rpm’s the bike is running at on those dark rides.
The next fix I had to do was find a permanent mounting place
for the license plate. You can see my
solution below.
The mount is made up from the remainder of the tail
light/license plate stalk that I cut
up to make the shorter tail light stalk earlier. I cut a small section out of the remaining
bottom portion and pounded it flat (see the detail picture below to get an idea
of what I cut out).
Then I located the center line and drilled two mounting
holes in the license plate bracket and then lined the bracket up below the tail
light which is clear on the bottom to illuminate the license plate (a rule at
least in Wisconsin that I know a few people have been pulled over for
breaking). I have to admit to using
standard nuts and bolts washers and lock washers for this. They are just so much cheaper than their
metric counterparts.
The next issue came up on a ride back home from work after a
night shift one morning but I want to start with the ride to work and work
forward from there. I had noticed that
as I was riding the bike to different places that the bike seemed to be having
a slightly harder time starting each subsequent time. Undaunted I started on my way to work that
afternoon. Normally on days that I work
nights I like to head into work much earlier to avoid the chance of traffic
headaches and afford myself a more Zen state of mind when I have to start my
workday. I started the bike and the starter
barely seemed to want to turn over but the bike roared to life and I rode the
bike downtown. I stopped over at Qdoba
for some free chips and queso that I had received as gift for my Qdoba card
registration anniversary (I used to eat a lot of Qdoba). Back at the bike there was no joy when I
thumbed the starter button the lights dimmed and all I got was a click the
battery seemed to be dying. Being that I
was already closer to work than home I decided to try and kick start the
bike. That worked right away, and I was
off to work but the ride was not going to be a good one. Twice as the idle dipped, the bike stalled
and this was in pretty steady traffic so both times I had to push the bike out
of the way to kick start it again. At one point when I was new to Oldbike I
told the guys on Caferacer.net
that I wanted to get rid of the electric starter to “save weight” to which one
of the members stated (I’m paraphrasing here) “…why would you do that? Do you
want to be the jackass who is holding up traffic while you try to kick start
your bike after you killed it? Or would you rather just thumb the button and
go?” I thought of that moment both times
as I wheeled the bike to the side of the road realizing that all those people
DID think that I was a JACKASS and that I would definitely have to figure out
what was wrong with my starter. I made
one more stop at a Ground Zero a coffee shop near my work and had to kick start
the bike when I left there and rode the two blocks to work where I had the next
12 hours to wonder whether or not I would make it home seeing as how the bike
had already stalled twice in traffic.
The next morning it was COLD…
...and I was tired. I
had brought a pair of riding pants to go over my jeans and an extra layer to go
underneath my jacket as well as some snowboarding gloves to wear rather than my
regular riding gloves this combination had worked well in the high 40s but 3
degrees above freezing is a whole ‘nother story. One thing that I hadn’t anticipated was how
hard it would be to lift my leg high enough to kick start the bike with the two
layers of pants on this was a chore.
Also I had left my gloves and helmet off for ease of starting, what I
hadn’t planned on was that it was so cold that the bike wouldn’t idle high
enough to run so every time I let off the throttle to put on my gloves and
helmet the thing died and I had to kick start it again, I did that twice before
I put on my gloves and helmet before kick starting the bike a fourth time,
hopping on and speeding off towards home.
The cold on the ride home was tempered by the fear that at any moment
the bike would quit on me and leave me stranded, and the half awake half asleep
haze that you are in after a night shift.
To make sure that this didn’t happen I kept the throttle at 2,000 RPMs
at all the stops as the bike seemed to die when the RPMs dropped too low. Luckily I made it home though when I looked
down I saw the top triple clamp bolt was gone.
I had never really checked the torque on it and it must have
been working it’s way out for some time and worked it’s way out on the ride
home helped along by all the high rpm stops to keep the bike running. Not spending too much time thinking about it
at that point I went inside to warm up and went to sleep.
Two days later I went and checked online and found that an OEM
replacement head bolt and washer would be around $7, not too bad but as this is
a budget project I felt obliged to see if I could find a generic replacement
bolt that would fit locally for less. I
did some internal measurements of the threaded portion of the steering stem and
my best guess was that it was a M12 fine threaded bolt and the thread depth
seemed to be about 20mm so I had my target I just needed to find one. Sadly my go-to place for fasteners Dorn True Value struck out on this one
they only had an M12X20mm in coarse threading.
So I stopped by the Menards near my house and found a M12X25mm fine
thread. I thought that this would work
if I took into consideration that I was measuring from the top of the steering
stem which was recessed a bit in the top triple clamp and adding a flat washer
to this and a lock washer I took a gamble and bought the only M12X25mm fine
thread bolt that Menards had.
Fortunately I was right and the bolt worked perfectly.
I also took the opportunity to look up all the torque specs
for the respective bolts in the steering system and to properly torque them
down. A cool thing was that the castle
nut tool that a friend of mine made for me years ago for my 2002 SV650s fit
perfectly onto it's 23 years older brother's castle nut too! I wonder if they use the same machine to make
those nuts?
Now the bigger issue was going to be what to do about the
starting issue I was experiencing. You
can’t do any good electrical diagnostic testing without a good, fully charged
battery. I noticed that the acid level
on my battery seemed a little low and since I had just
recently bought Oldbike’s battery and it was a Yuasa a “good brand” I
called the place I bought it from the Engelhart
Center and asked if the low acid might be causing what I was experiencing
they weren’t sure but they offered to re-fill the battery, fully charge it and
test it to make sure it was good free of charge (even thou later we would find
that it was 10 days outside of it’s year warranty).
I thought that was really cool of them and in the end the
battery came back to me testing good so that was not the issue but something
was draining the battery.
After finding out that the battery was good I set about
fixing a glaring issue that has bothered me from the first time I looked at the
bikes battery closely for the first time.
The positive wire from the battery to the solenoid was very frayed and
looked like it had been cut shorter and had new ends put on it at least once if
not twice and due to the age and the angle that the wire had to bend the wires
were brittle and breaking.
I also wanted to replace the old tube style main fuse with a
blade style fuse.
The OEM replacement was
listed as unavailable but Motorcycle
Performance at least had a single wire replacement that I could modify to
be like the OEM one. You can see it in
the picture below along with the in line blade style fuse replacement I used.
The only issue that I talked
trhough with an EE friend of mine was the gauge difference between the
connectors I wanted to splice at each end of the in-line fuse. After some discussion we came to teh
conclustion that being that the only fuse in the system is that fuse that and
all of the other wire is the same smaller gauge that it shouldn't hurt. I am still open to comments on this as I
don't want to be stepping backwards in reliability the blade style fuse is
supposed to be an enhancement so if you have comments or suggestions on this
front feel free to share them.
Of course I solderedall the
connections.
I thought about doubling the
connectors back but the with the extra length of wire I added I figured why add
the extra stress to the wire so I civered them with shrink tubing as is.
The last thing I needed to do
was to remove the factory applied shrink tubing from the replacement wire and trim
back some of the shielding cable to attach the break-off for the bike power
supply...
...solder the connection...
...and re shrink-tube the
connector and wires.
Here is a shot of the
"new" wiring.
And here it is back on the
bike.
For fun I took a picture of my life's
worth of odds and ends that I have collected throughout the years. This is all
the stuff that as a man you keep because you "might need it" at some
point. Am I ever going to need a steering wheel puller or a lock plate
compressor? Probably not, but it's in there :-)
The next test I did was to see if the battery was being
charged by testing the volts through the battery as the bike was running.
I used this helpful YouTube video as a guide on how to do
the test.
Below you can see my test and results.
Right now I am poring over “The Stator
Papers” on GS Resources.
Stay tuned for my next update where I will start working
through the different array of tests to run down my charging system issues.
Thanks as always for reading!
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